Knight-Morley Corp. v. Employment Security Commission

86 N.W.2d 549, 350 Mich. 397
CourtMichigan Supreme Court
DecidedNovember 26, 1957
DocketDocket 36, Calendar 46,779
StatusPublished
Cited by22 cases

This text of 86 N.W.2d 549 (Knight-Morley Corp. v. Employment Security Commission) is published on Counsel Stack Legal Research, covering Michigan Supreme Court primary law. Counsel Stack provides free access to over 12 million legal documents including statutes, case law, regulations, and constitutions.

Bluebook
Knight-Morley Corp. v. Employment Security Commission, 86 N.W.2d 549, 350 Mich. 397 (Mich. 1957).

Opinion

Sharpe, J.

(for affirmance). Defendant Norwood H. Beier and others, together with the Michigan employment security commission, appeal from a judgment of the circuit court of Ingham county denying Norwood H. Beier and others benefits under the Michigan employment security act.

Certain facts are undisputed and are as follows: During the year 1953 plaintiff corporation operated' a plant in Richmond, Michigan, and employed between 150 and 200 employees in the manufacture of die castings and brass objects. On August 31, 1953, the defendants, now claimants for unemployment benefits, were employed in a buffing room approximately 25 feet wide by 85 feet long. This room was equipped with 10 buffing jacks, 3 rotary automatic buffing machines and a straight line unit. The buffing room is responsible for polishing objects, and this is accomplished by placing the object against a revolving wheel. This wheel removes particles from-the object and brings it to a high polish and luster. As a result of this process, abrasive particles, lint. *399 and dust are thrown from the wheel. The. buffing room had an exhaust system. Each of the 2 wheels of the huffing jack was partially enclosed by a hood. From each hood a 4-inch diameter, pipe led up to and connected with a 24-inch diameter pipe running into the buffing room. At the end of this 24-inch pipe there is a paddle-type fan which created suction to draw particles from the buffing wheels into and through the exhaust system.

On Friday, August 28, 1953, a fire occurred in the electrical system of the exhaust unit and the employees were required to go home because it was not operating properly. The following day the machine was repaired. However, by inadvertence, certain wires were crossed, causing the paddle wheel to revolve in the opposite direction.

On Monday, August 31, 1953, the day shift buffing employees started work at 7 a.m., but were sent home after working 2 hours in order to permit cleaning of the blowers. The afternoon shift reported to work in the buffing room at their normal starting time of 3:30 p.m. The day was hot and muggy. Shortly after work started a dispute arose as to the condition of the blower. The president of the corporation made an investigation and concluded that the machines were working properly and ordered the men to continue work. The men informed the corporation that they would not work unless the blowers were repaired. The men left the plant after working approximately 2 hours. Prior to leaving the plant, the men were informed that their leaving would be construed as quitting their jobs. The following day, September 1st, the blowers were repaired after the day shift left, and when the afternoon shift employees reported for work on September 1st they were informed that their cards had been pulled and they were considered as having quit their employment.

*400 On October 19,1953, a notice of determination was mailed holding that claimants were not discharged for misconduct with their work on August 31, 1953, and that they were not disqualified under section 29 of the act. An appeal was made to the referee who found in favor of claimants, holding that claimants did not leave their work voluntarily without good cause. The employer appealed to the appeal board. The appeal board adopted the findings of the referee.

The employer then appealed to the circuit court of Ingham county. The trial court entered an order denying claimants unemployment compensation. In an opinion the trial court stated:

“This court has reviewed the rather lengthy record and is of the opinion that the majority opinion of the appeal board is contrary to the great weight of the evidence. The record clearly indicates that the employees voluntarily left their work because of the fact that they only wanted to work for 2 hours, the same as was done by the morning shift. The testimony of Mr. Harsch, the union president, clearly shows that the employees did not intend to work more than the 2-hour period. It was somewhat oyer an hour after they started work when they started complaining that the blower system was not operating normally. The record shows that even though the fan was not turning in its usual direction it was still operating efficiently and there was enough suction to carry away the dust, lint, et cetera. The record shows that the day shift worked full 8 hours on September 1st, and that the blower system was operating efficiently during that period, and that no changes had been made in the system from the time the claimants walked out on August 31st.
“The record indicates that the claimants did not want to work longer than 2 hours, as was done by the morning shift, and used the blower system as their excuse for not working over the 2-hour period.”

*401 Claimants appeal and urge:

“That the lower court erred in fact and in law in reversing the decision of the appeal board of the Michigan employment security commission that the defendants and appellants were entitled to receive benefits without disqualification under the provisions of section 29(1) (b) of the Michigan employment security act, said judgment of the lower court being contrary to the great weight of the evidence and erroneous in law.
“That the lower court erred in failing to remand the proceedings to the appeal board for the purpose of taking further testimony from Dr. "William Fred-ericks, a recognized expert in the industrial hygiene field, concerning the condition of the ventilation system claimed by appellants to have been the cause of the cessation of work by claimants.”

Additional facts helpful to decision are as follows. Plaintiff’s blower system had a rated capacity of 13,500 cubic feet of air per minute, which was 50% in excess of the 9,000-cubic-foot capacity required by law. (CL 1948, § 408.80 [Stat Ann § 17.39].) It is undisputed that a paddle-wheel type fan will pull or displace the air no matter which way it rotates. Lloyd Utter, the expert witness produced by appellant, testified:

“The paddle-wheel type of a fan will pull the air rotating either way. It would reduce something between 10 and 50% depending on how much it has to buck the contour of the system. * * * Reversing it would not affect it. * * * I will state, if it is a straight pipe, it doesn’t make any difference which way the fan blows.”

The statutory provisions involved in the case at bar are as follows :

“(1) An individual shall he disqualified for benefits: (a) For the duration of his unemployment in all cases where the individual has: (1) Left his work *402 voluntarily without good cause attributable to the employer or employing unit, or (2) has been discharged for misconduct connected with his work or ior intoxication while at work.” (Section 29 of Michigan employment security act, CLS 1952, § 421.29 [Stat Ann 1953 Cum Supp § 17.531].)

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Bluebook (online)
86 N.W.2d 549, 350 Mich. 397, Counsel Stack Legal Research, https://law.counselstack.com/opinion/knight-morley-corp-v-employment-security-commission-mich-1957.