Sutton Drilling Company, Inc. v. Universal Insurance Company

335 F.2d 820
CourtCourt of Appeals for the Fifth Circuit
DecidedNovember 4, 1964
Docket21000
StatusPublished
Cited by5 cases

This text of 335 F.2d 820 (Sutton Drilling Company, Inc. v. Universal Insurance Company) is published on Counsel Stack Legal Research, covering Court of Appeals for the Fifth Circuit primary law. Counsel Stack provides free access to over 12 million legal documents including statutes, case law, regulations, and constitutions.

Bluebook
Sutton Drilling Company, Inc. v. Universal Insurance Company, 335 F.2d 820 (5th Cir. 1964).

Opinion

JOHN R. BROWN, Circuit Judge.

The question in this case is when is a blowout not a blowout. More accurately, the question is whether the occurrence damaging, if not completely destroying the well being drilled, amounts to a “blowout” as defined in the policy. Upon the jury verdict, the District Court determined that it was not a blowout' and entered judgment for the Insurer. The Assured appeals. We reverse.

At the heart of the whole controversy is the policy definition of a blowout. 1 Since that inevitably leads the parties and us into a comparison of this case with our decisions in Georgia Home Ins. Co. v. Means, 5 Cir., 1951, 186 F.2d 783, and Fidelity-Phoenix Fire Iris. Co. v. Dyer, 5 Cir., 1955, 220 F.2d 697, it is helpful to parallel the policy definitions in Means 2 and Dyer. 3 Unlike those cases, this one was tried to a jury whose verdict in response to special interrogatories and a general charge, F.R.Civ.P. 49 (a) reveals precisely the determination of the subsidiary elements of the blowout definition. 4 To the extent that any one or more of these represent questions of fact, it is necessary — if the Assured is to carry the day — that' it convince us that its motion for instructed verdict and for j.n.o.v. based thereon, F.R.Civ.P. 50(b), should have been granted.

We defer for the moment any discussion of whether the facts gave rise to *822 diverse inferences warranting jury submission to substantiate the verdict (note 4, supra). The trial itself was a short one in which for all practical purposes, the facts recited were uncontradicted. For our purposes, they may be briefly summarized and for this purpose we draw heavily on the briefs for this paraphrase.

During the month of April 1961, the Assured was engaged in the drilling of an oil well known as Sol West, Jr. No. 1, in Live Oak County, Texas. The well was to have been drilled to a total depth of approximately 10,000 feet.

On April 22, while drilling in a sand formation at a depth of 9,320 feet one of the crew members noticed that mud was increasing in the pits, indicating that more mud was coming out of the hole than was being pumped into the hole. As it was probable that the drill stem had encountered a subsurface formation which was exerting more pressure on the column of drilling fluid than the hydrostatic pressure was exerting on the formation, the tool pusher in charge of the drilling operation had the driller pull the drill stem, and the crew began to weight up mud in an attempt to control the subsurface formation pressure. The rate of return of the mud rapidly increased, however, and within about ten minutes the fluid began to flow up over the bell nipple in the top of the casing erupting approximately 10 to 15 feet above the derrick floor. As he feared a violent eruption of mud and gas, the tool pusher ordered the blowout prevent-er 5 *closed.

After closing the BOP, the crew continued to pump heavy mud into the hole, but rotation of the drill pipe could not be resumed because any attempt to turn it with the BOP closed would damage the rubber bushings and make it ineffective.

Efforts to equalize the circulation of the drilling fluid continued for a period of from four to six hours after the initial eruption of the drilling fluid from the well. Considerable heavy mud was pumped into the well, but it did not overcome the pressure imbalance from the subsurface formation. It was then observed that salt water was starting to come out of the choke line. 6 The tool pusher concluded from this that the excessive pressure was forcing the heavy mud out into some formation down the hole somewhere, and that the well was cleaning itself of the drilling fluid and gas causing the walls of the hole to cave in.

All efforts on the part of the crew to restore circulation failed. They were apprehensive that the hole or bore of the well had bridged over 7 causing the drill pipe to become stuck. Of course, no test could be made with the BOP closed. To determine the situation as to the drill pipe, the BOP was opened. Immediately a volume of mud in a column the diameter of the surface casing (10%") was expelled out of the well approximately 20 feet into the air. With this expulsion continuing, unsuccessful attempts were made to rotate the drill pipe or move it. This proved what the tool pusher apprehended, that the drill pipe had become stuck because of the bridging over of the hole. The BOP was immediately reclosed. About this time, those in charge concluded that it was not possible to resume the previous drilling operation and the decision was then made to attempt to kill the well. Approximate *823 ly 700 barrels of drilling mud costing $15,000 to $20,000 was pumped into the hole. This was ineffectual in overcoming the reverse pressure from the subsurface formation. It also indicated quite positively, from the loss of the fluid, that the mud-fluid was being forced out into one or more subsurface formations with undoubted damage to the wall of the hole. Efforts were then made to cement off the bottom of the hole. As we read the testimony, the initial hope was that the cementing would enable them to recover the drill pipe and then by accepted procedures, drill through or past 8 and thereby complete the well substantially as originally planned. On the first attempt cement was pumped down the drill ■pipe, out through the bit, and up into ■the annulus. Because of extremely high pressures, which the Assured estimated to have been two to three times that normally encountered (4500 psi), the cement would not set at or near the bottom ■of the hole (approximately 9200 feet). The record indicates that at least one and perhaps two more attempts to cement were made. The last attempt successfully plugged the annulus at approximately 7300 feet. 9 This kept the gas pressure from escaping in the annulus, but in the meantime the gas pressure was still being exerted inside the drill pipe. The hydrostatic pressure of the mud being pumped into the drill pipe and perhaps a surface valve prevented the escape of this gas (and fluids), but this condition could not be continued indefinitely. So it was decided to freeze the mud in the drill pipe by packing dry ice around the outside of it. With that frozen “plug” in the drill pipe, they were able to cut off the pipe, install the “Christmas tree,” and complete it as a shut-in gas well. As a result of this incident, the Assured lost drill pipe, drill collars, 10 and other undisclosed equipment of an agreed value of $33,-266.62. 11

It is undisputed that the BOP did hold. When it was first closed, it functioned properly.

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335 F.2d 820, Counsel Stack Legal Research, https://law.counselstack.com/opinion/sutton-drilling-company-inc-v-universal-insurance-company-ca5-1964.